Show simple item record

dc.contributor.advisorRomdhane, Lotfi
dc.contributor.advisorGhommem, Mehdi
dc.contributor.authorAl Hussaini, Osama
dc.date.accessioned2023-09-19T05:55:19Z
dc.date.available2023-09-19T05:55:19Z
dc.date.issued2023-05
dc.identifier.other35.232-2023.33
dc.identifier.urihttp://hdl.handle.net/11073/25349
dc.descriptionA Master of Science thesis in Mechanical Engineering by Osama Al Hussaini entitled, “Design, Implementation, and Performance Analysis of Actively”, submitted in May 2023. Thesis advisor is Dr. Lotfi Romdhane and thesis co-advisor is Dr. Mehdi Ghommem. Soft copy is available (Thesis, Completion Certificate, Approval Signatures, and AUS Archives Consent Form).en_US
dc.description.abstractThe new technology of morphing wings has potential to impact the aeronautic industry as it greatly reduces the associated operational costs. This is achieved by drastically lowering the fuel consumption of aircrafts and enhancing their flight performance. Morphing wings have the capability to change their shape dynamically to achieve numerous aerodynamic characteristics that can fit different flight missions and operating environments. In this Thesis report, we investigate the potential enhancement in the aerodynamic performance of morphing wings made of NACA0012 airfoil. An aerodynamic analysis was first carried out to identify optimum morphing configurations. The obtained wing profiles showed capability to significantly increase the lift coefficient and reduce the drag coefficient, resulting in a high lift-over-drag ratio. The numerical analysis was conducted by interfacing the aerodynamic simulation tool XFOIL with MATLAB to obtain a user-friendly tool that eased the aerodynamic analysis and the optimization study. Based on the morphing shapes obtained from the optimization analysis, a morphing wing prototype was developed and tested. The prototype uses the Fish Bone Active Camber (FishBAC) mechanism to induce morphing in the trailing edge portion of the wing structure. Moreover, the FishBAC used in this Thesis was enhanced by adding an additional degree of freedom, which is an unprecedented contribution to this particular mechanism. The second degree of freedom significantly improved the morphing efficiency. Wind tunnel tests were conducted on the developed wing prototype to inspect the lift generation under various airspeeds and morphing configurations. Experimental measurements showed evidence of 60% increase in the lift thanks to the incorporation of morphing obtained from the optimization analysis. The experimental results showed also qualitative agreement with their numerical counterparts.en_US
dc.description.sponsorshipCollege of Engineeringen_US
dc.description.sponsorshipDepartment of Mechanical Engineeringen_US
dc.language.isoen_USen_US
dc.relation.ispartofseriesMaster of Science in Mechanical Engineering (MSME)en_US
dc.subjectMorphing wingsen_US
dc.subjectFishBAC mechanismen_US
dc.subjectWind tunnel testingen_US
dc.subjectAerodynamic analysisen_US
dc.subjectMorphing shape optimizationen_US
dc.titleDesign, Implementation, and Performance Analysis of Activelyen_US
dc.typeThesisen_US


Files in this item

Thumbnail

This item appears in the following Collection(s)

Show simple item record